-
JRenta posted an update 5 years ago
I ran an example servo script that comes in Arduino Software to test the wrist servo and it works fine but when I use the NervoBoard to control the Wrist, it seems to not have enough power or maybe the impedance is not tuned correctly. I have the MRL Servo test sweeping from 0 to 180 and the wrist moves but just a tiny bit. Anyone experience this problem?
JRenta
@jrenta
Active 1 year, 4 months ago
I am having an issue with the Speech in MRL. MRL seems to respond just fine for the first couple of minutes but then does not respond at all and I have to restart mrl. Refreshing the browser does not help. I think it has something to do with it try to search online for answers and then gets hung – I’m not sure… I’ll add more details later. If […] View
I figured it out. The MG 996R Servo was placed backwards and got hot and now theres a short across the motor inside the servo. Easy fix is to replace the motor.
Hello,
How do you power your NervoBoard?
Do you have a voltmeter to check if you have the correct voltage coming to the servo?
I power the NervoBoard with a Power Supply that is at 6V Constant. I’m not sure what was the root cause but I was able to replace it with an HS485B with no problem.
Hello,
Possibly your extracted potentiometer that is damaged or a bad soldering on the potentiometer wires.