• Thomas Wurm posted an update 10 years, 1 month ago

    first test with an arduino sketch

    • i killed the jaw servo in my first test but i replaced it in this video

    • What servo did you use for the jaw? I have burned a few of them, MG995, MG946R, MG996R… The torque needed to action the jaw, and the movement repetition cause great stress on the servo. Bob Houston has been using a HS-311 servo since he started his built and says he never had to replace it.
      Might be worth trying.

      • the servo was a MG 946
        but it was a programming error in my arduino sketch, I did not use myrobotlab
        got it just today installed and trying to find my way